Hay needs to come in, really it does

Since Tex did not answer my text he is not coming out. This does not change the fact that we need to get the hay inside the barn. So Annmarie and I headed out first thing Saturday morning to get it done! She was going to drive the pickup pulling our trailer and I would load and unload hay into the barn. The culverts are only 10 feet wide and the trailer is 8 feet wide. This meant that Annmarie made me drive it across the culvert. I chose to cross over the new culvert as the old one is elevated and starting to crumble, the rocks are falling off. I really need to fix it but its a low priority. Hay and fencing are number one and two right now. The bales are kind of randomly spaced and close together so Annmarie had to weave in and out of the bales so I could pick them up. Using hay hooks they are not hard to pickup and the trailer and pickup had no trouble hauling them.

I did the first two loads without a hitch. I had Annmarie trained to start and stop by merely hollering “K”. It was taking about 1.25 hours per load.

So it’s load three time and I almost have the trailer full when Annmarie tells me the pickup engine is smoking. Smoking is not a good sign for an engine. I popped the hood and there is a radiator leak in the top right corner of the radiator. Now, I had been having some issues with the pickup heating up over the last month but I thought it was a thermostat issue, I was wrong. I had her park it and we went inside. Once the engine cools off I will fill it with water and drive it back to the house. We can then fill it up to the brim and drive it to the shop for repair. Now this is not totally unexpected but I still need to get hay picked up!

Tex had asked me if we could pull the trailer with the tractor but I told him I was unsure if the tractor could haul that much weight. I do have a draw bar on the back of the tractor. Now that I have no choice I decided to try the tractor. The holes in the draw bar are too small to insert a 2 5/8″ ball. I ended up going to D and B farm supply store and buying a bar for the three point hitch and a stinger with three sizes of balls with a pin that allows me to turn the stinger and change my ball size. This allows me to use the three point and it pinches it in place which allows me to lift the trailer with the three point. I would need to figure out an upper attachment to allow me to use it without getting off of the tractor. This was going to require more thought and time and my current method worked! I did one more load but as I was getting sick thanks to Tex or Annmarie I went inside cleaned up and went to bed.

The hay still needs to get into the barn. Tex messaged me, he is not coming on Sunday as its Father’s Day. I foresee a day spent on the couch being miserable.

Till the sun goes down

It has been a long week. Tex got the plague! No man is immune from a good virus, I blame his mother for giving it to him. He was out on the two days needed to ride the baler and put some hay out! So I was going to work, coming straight home, changing clothes, grabbing a quick bite to eat, some water and hitting the fields until dark. It was not all fun and games, there is a definite learning curve to using new equipment and especially when you have never put up hay before. I jammed the thing full a few times and had to dig it out by hand. I backed into a completed bale and caught the string and sucked it up and wrapped it around the guts of the baler. This took a while to get undone. I only sheared one more shear bolt the rest of the week. I would come inside at dark, cleanup and go to bed to wake up and do it again.

Since there are no microbalers in our area, I bought normal haying twine, but it will not fit inside the compartment designed to hold it. So we just set it between the baler and the quick hitch. It didn’t even need strapped down, it would just ride there and pull itself out. We went through ten rolls of baling twine.

One night was spectacular! I had jammed the baler for the third time and just called it quits. I was getting ready to head inside when I noticed the view, it does set things into perspective. It was a good way to end a frustrating day.

Tex finally healed himself and came out to the house on Thursday. We were only about 50 bales from completion and would need a spot to put the bales so we worked on lining one side of the barn with 2×6 boards so that the round bales would not touch the outer walls. I had plans on buying some pretty boards but at the rate we are burning through cash I opted to use some boards that we already had on hand. We used boards left over from building the bull enclosure. Probably a much better deal all around for everyone. We got ten feet into the air and decided to wait on installing the higher boards until we had stacked the hay up to the top board. This would then allow us to just stand on the hay pile and install them without trying to use them as ladders, hold on and then screw them in place. This does require some balance and dexterity and muscles which could be better utilized in stacking hay. Tex jumped onto the tractor and finished out the last of the hay while I ran to town . Slim had come out the day before and knocked down 90% of the grass in our front yard. This was a needed task and at the rate we keep Tex busy neither one of us were going to get to it.

I had Tex hook the hay mower back up and Thursday evening I opted to drive down and start haying down by the school house. Two passes and I heard some loud whine from the drum mower. Now I had just hit a hidden 2” pipe with the mower on the last pass. I discovered that I had ripped off all the blades from one of the drums. All of the bolts were missing! I even managed to find one of the blades. So now I am going to have to order new bolts and blades for the loaner mower. I also had to disconnect the PTO shaft from the mower and dig out all the loose grass that had wrapped around the head and was smoking from the friction. I did mention this is a loaner? I called the place this morning first thing and was told this is their busy season and to be patient they would get back to me. Well they did not get back to me today and I cannot cut any more fields for hay until I get the mower fixed. So tomorrow I will try and order the parts I need and we will see how long it takes them to get to me.

We ended up with 1050 bales that weigh about 45# each, so about 23.5 ton in 8 acres. I have about another 6 acres down by the school house to cut still. We will buy some alfalfa this year and plant two more fields this fall. I am pretty sure we are going to plant 7 acres of Sainfoin and then more grass fields. Our big push now is to pick up all those bales by hand!

Micro Hay equipment, its a thing

Well Tex came out this morning and while we were eating breakfast “Slim” came out. She is Tex’s little sister and she has agreed to dig out the chicken coop and the barn and do a few odd chores this summer. I set her up with instructions on how to clean out coop, we found all the tools and I got her some bleach, a rag and a bucket for after it got cleaned out. Tex and I went out to the machine shed to attempt to get the micro baler hooked up. This proved difficult at best as the first PTO shaft was too long, so we added the quick connect to get three inches more away from the tractor. The PTO shaft just did not want to go on. We then had to change out the posts and adjust everything to get the dang thing lined up correctly. We also had to put in a quart of gear oil into the baler. I was a little surprised by this as the thing is brand new and has not been leaking at all. We managed to read the instructions a couple more times and drove up to the second field to try it out.

Tex went with me as we figured there would be a learning curve. This was a major misstatement as we managed to only make two bales in the first hour and could not get either one of them wrapped in twine. They were totally naked. We managed to shear off two shear bolts and discover that a pair of spring wire pliers are needed to correct this issue. I do not own a pair of said pliers so I did it by hand, which is never fun. I finally got three bales done correctly and Tex went off to work on the machine shed while I tried to figure it out.

Tex outsmarted himself as doubling the row widths caused a ton of problems. The rows are too wide and too much material is present. We would have been way better off had he not done it. It made baling it a lot harder. I spent 3 hours on the tractor and got 119 bales done. Two boxes of baling twine are not going to be enough. We are using a lot of twine. I managed to mess up two bales and had to lift the dump part manually twice. The second time I had to go get Tex, damn thing is just getting heavier and heavier.

Each bale is supposed to weigh around 50#, I went down to the machine shed to get Tex so I could show him how to bale and give him some tips to avoid issues. He was working with Slim and they had gotten 8 sheets of plywood up on the walls. I showed Slim a few more things I wanted done in the chicken coop and she set right to work. I had told her first thing this was only a one day job and she did it! She just dug in and did the job!! So nice and refreshing.

I ran back to town and got 10 gallons of diesel and 10 more rolls of twine so Tex will be able to hit it hard first thing at 0900 tomorrow. When I come home from work I will relieve him and go until dark. The race is on now to get it all done. It does not look like we already have almost 5 ton of hay baled. I think we are going to have over 1000 bales in just the first field only.

It must be even

It had rained the days before so we did not want to cut any new hay. Instead we planned on turning hay. I had a funeral to go to so we got Tex all set up with our new 5 foot power rake. He will turn all the hay this Saturday. This rake will let you pile it all up into a row. I had visions of Tex just following the rows that the mower created. he did one better! He went down one side of the row then at the end of the row he turned around 180 degrees and went the opposite direction allowing the row to double in size and cut the number of rows in half. This was very clever and not something I would have thought of had I done the turning.

Before I left in the morning Tex and I planned out our needed improvements to the machine shop. One of the rafters is broken, we need a bunch of plywood to line the hay room to keep the round bales in and the loose hay out of the new gravel area. We also need to install the bolt and screw organizers that were laying on the floor of the machine shed. I need to get all the bolts and screws organized and out of the multitude of drawers I currently have them in. I am also going to hang some bin organizers on one wall. I need to mount these to a sheet of plywood, so we will be hanging a few sheets up on the walls for future use. We also need to make legs for the new free countertops I managed to snag on the way home this week. Every once in a while those “Free” signs are a big win.

I went to my least favorite big box store and picked up plywood and lumber with a few Knick nacks. I had to wait 30 minutes for help loading plywood as there was only one guy who could do it. There are reasons I dread Home Depot, but I spend so much money there I get the zero interest for 6 months on my charge card and always pay it off in time. I love that deal!! Plus on Saturday at 1600 there is no other place in the area open to buy lumber.

I knew I needed some more baling twine, but with micro equipment I was unsure where I was going to get it. The salesman on the phone seemed to think I could get it anywhere. So I found it at a local store and bought two small, 5000 feet rounds. They did not have Jute cord like the free roll I got with the baler but they had lots of types of plastic cord to pick from. I was not sure if they would fit but its all they had and something is better than nothing.

When I got home and published the blog last night Annmarie spotted the uneven gates on the new stretch of fence. She mentioned that would need to be corrected tomorrow. I told her hay came first but I would think about how to fix it without spending 10 hours reworking two rock cribs.

Haying virgin

The farm parts place came through in spades! My new driveshaft came in on Monday and I was able to pick it up that evening. Now it was 28″ and would need to be cut down but I had purchased a grinder that went with the new 60V DeWalt battery. It is amazing! There is no noticeable difference between the battery grinder and a plug in one other than pure convenience. Electric tools had to be able to get there eventually.

On Tuesday afternoon I cut the driveshaft, attempted to install it and had to cut another 2″ off to make it fit properly, this took a while. I was now ready to cut some hay!

This is me ready to cut some hay. I spent another 30 minutes on the internet and watching YouTube videos trying to figure out how to rotate the drum to behind the tractor for transport. I never did figure it out. Yes I read the instruction manual, but it was originally written in Italian and then translated into English. There were about 20 pages of how not to cut your hands or feet off because the mower blades are rotating. So this means I cannot go through narrow gates, it is possible but it does limit the gates that I can use.

I fired up the drum mower and started to mow in the cow pasture. I figured it was a great place to start and work out the kinks. Yes, there is a learning curve on where you can drive and how fast you can drive. After about an hour I started to hear this thunking noise. I finally stopped the mower, lifted it and waited for the blades to stop. The blades actually take about a minute to stop rotating and after hitting a rock and slicing it in two I figured out why the manufacturer had 20 pages of instructions on how not to slice off a body part.

There was a skid plate off of the bottom of one of the two drums that had come loose and was held on by a single bolt. Three bolts had already fallen out. I attempted to take a bolt out of the intact side but was unable to get one loose. So I had to take the loose one out, it came out with my fingers and then I went to Pendleton. Everything is from Italy, so it’s all going to be Metric. I had my fingers crossed and hoped I could find replacement bolts. I found 6, I needed 3 but they only had them in alloy not stainless steel like the ones that fell out. So I grabbed all the alloy they had and went home. I was putting the third one in when I realized something was different about the drum plate I was installing and the intact one. There were 14mm spaces between the bottom of the drum mower and the skid plate. There were no spacers when I found it. So, I had to go back to town and find something that could act like a spacer. I did and managed to get them installed. This is the loaner mower!

I started mowing again and just kept going until 2230 at night. I am definitely going to have to invest in some kind of aftermarket lights for the roll bar. There is 300# of antique tractor weight discs in the tractor bucket to offset the mower weight. So when I get the bucket high enough into the air to see with the headlights the tractor becomes very top heavy. I almost tipped it over twice. If I had roll bar lights I could keep the bucket closer to the ground and it would be much safer.

I came back on Wednesday and was able to finish both fields by 2100. So about 11 acres cut in 11 hours. Now I think in all reality that number could be 11 acres in 6 hours without the breakdowns and learning curve. Its supposed to rain.